Running the Ecotech EZ Variable Speed Pool Pump Motor - GFCI Breaker Issues and Resolution

I've been upgrading my pool pump system with a variable speed motor from Emerson / Nidec / US Motors - the 3HP Ecotech EZ motor. I've described installing the motor on the pump, and the upgrade of the pool piping from 1 1/2" diameter to 2" diameter for better flow and lower restriction.

Ecotech EZ Variable Speed Motor installed on the Jacuzzi Magnum 1500 Pool Pump
The night that I finished the last of the 2" piping was when I reinstalled the salt chlorination cell. Then it was time to start up the pump for first time. Power on - then 2 seconds later the GFCI breaker feeding the sub panel in the pool shack tripped, and an error message appeared on the motor's LCD screen - blocked pump. The motor has a protection feature if the impellor gets blocked - it will prevent the motor from forcing against a blockage. I reset the breaker and tried a few times to get the pump running - then realized that I had installed the motor adapter plate backwards - jamming the impellor against the seal plate. So - 11:30 at night, and I pulled the motor from the pump and flipped the adapter plate, reassembled the pump and......the GFCI breaker still trips - but I no longer have the blocked pump error message on the variable speed control panel.

Ecotech EZ Motor Control Panel
The manual for the Ecotech EZ pool pump motor very clearly states that if you want the motor protected by a GFCI breaker, the pump must be installed on a dedicated GFCI circuit, not shared with other electrical loads. This posed a problem with my electrical system - my pool shack sub panel has 6 circuits - 4 15A lighting and power outlet circuits - one of which is the pool lights, and two 2-pole 240V circuits - one for the thermopump heater and one for the pool pump. When I moved into this house 3 years ago - only the pool light circuit was protected with a GFCI breaker. So - to upgrade the protection for the most economical cost - I protected the entire sub-panel from the feed from the house panel with a 40A 2 pole 240V GFCI breaker. The implication  of the requirement to have the Ecotech motor on its own dedicated GFCI circuit was to remove the GFCI breaker from the panel feeding the sub panel, and convert all the breakers on the sub-panel to GFCI breakers - an expensive upgrade. To try to avoid all this - I tried to get the pump to work with the GFCI breaker on the house panel - but even removing all the other loads on the sub-panel was causing the feeder GFCI breaker to trip every time I tried to start the motor. 

Ecotech EZ Motor Upgrade on Jacuzzi Magnum 1500 pump - with 2" plumbing upgrade
To get the motor running - I removed the GFCI breaker from the sub-panel feed. It started and ran fine, but with no GFCI protection. When anyone went near the pool, I shut off all the breakers on the sub-panel for safety, but this wasn't practical as a permanent solution. Incidentally - I did some research on other variable speed pool pumps - such as the Pentair Intelliflo pump - and it's installation manual also requires a dedicated circuit if the pump is to be protected with a GFCI breaker. 

I had two 15A single pole GFCI breakers from the original installation, which I put back into the sub-panel. Then I purchased a single 2 pole 20A GFCI breaker for the pool pump circuit. I installed this on the sub-panel, and it worked fine. Then I installed a second 2 pole 20A GFCI breaker for the thermopump. 

The point of this whole discussion is to warn anyone considering this variable speed pump upgrade that there may be electrical implications beyond just swapping the motor. Also - it's important to state that you should have this electrical work performed by a licensed electrician - or have a licensed electrician inspect your handywork if you decide to do this yourself. You want to ensure that the electrical systems are safely installed and will protect your family and friends from an electrical fault.

One other issue that I've run into is that I had my salt chlorination cell transformer wired with my pool pump motor - but I've had to separate the circuits in order to get the GFCI breaker for the pool pump to work. Also - the pump needs to be powered on all the time - the pump timing is now controlled by the intelligent controller on the motor, and not my central pool automation system. So I've decided to control just the salt chlorination cell from my central pool automation system - I'll program it to run on a function based on the length of daylight since chlorine degradation is a function of sunlight - and run the pool pump separately using the timer on the motor controller. I still have some wiring to get this up and running - if I run into anything interesting - I may do a separate post on this.

Once I got the electrical issues sorted out, the pump has been running now for about 2 weeks. I did some testing to check the current draw on the pump at various pump flows. The control panel modifies the pump speed as percentage of flow, and not as percentage of speed changes. Since the pump runs with a single set of programming from the factory, and every pump installation will be different with its own piping head - the percentage of flow settings on the motor will only be approximate on any system. 


What's interesting about this graph is that I can run at 75% flow consuming only about half of the full speed motor current, or I can run at 60% flow consuming only about a third of the full speed current. I wish I had taken the motor current measurement of the original single speed motor on the Jacuzzi Magnum pump - this new permanent magnet motor should be much more efficient at full speed. For the past two weeks I've been running the pump 24 hours per day, at 50% speed consuming less than 1 Amp of current. At this speed the sand filter backpressure is only about 3 psi - the power savings are impressive, and the filtration is very effective - water is crystal clear and my salt cell is performing well.

Measuring power draw of the Ecotech EZ motor using the Klein CL1000 clamp meter
Another feature of the variable speed motor is to be able to fine tune the motor speed to your vacuum and vacuum hose length, to avoid cavitation of the motor. On my previous setup with the single speed motor - the motor would cavitate whenever I was vacuuming. This would cause the pump to periodically lose prime, and suction on the vacuum. In addition, whenever I was vacuuming to waste early in the season to rid the pool of dead algae, the single speed pump was always running at full speed and drawing down the water level very rapidly. Now I can vacuum to waste at 40% flow - greatly reduce the loss of water and increase the time that I have to vacuum more effectively. I also expect that I'll be able to tune the motor to the barracuda automatic vacuum for peak performance, without using the bypass valve. 

Ecotech EZ Motor - Timer Controller is mounted directly on the motor housing
So - with the exception of the surprise expense on the GFCI breaker upgrade on my sub-panel - I'm very satisfied with this pump motor upgrade. My pump running at 50% flow is very quiet - I can't hear the motor at all outside the pool shack, and my neighbor's pool pump makes more noise now than my own. One other thing that I like a lot about this upgrade is the performance of the Jandy multiport valves - much easier to actuate by hand, nice clean looking installation. This is a positive upgrade - and I hope to see the results on my electricity bill at the end of the summer. 

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Ecotech EZ Variable Speed Pool Pump Motor - Pump Installation and Piping Upgrades

Now that the pump is assembled with the new Ecotech EZ variable speed motor, it was time to get at the piping upgrades to help improve the overall system efficiency. I had a few serious weaknesses in my pool piping, particularly on the suction of the pool pump, and the piping feeding and exiting the thermopump.

Jacuzzi Magnum 1500 upgraded with Ecotech EZ Variable Speed Motor, Suction Side Piping Completed with 2 Jandy Valves
The existing pump piping layout wasn't very well done - it wasn't particularly efficient, and probably contributed to the pump cavitating any time the vacuum port was used. Note the vacuum port routing - which enters from the top right - 90 degree elbow, ball valve, 270 degree sweep, 90 degree elbow down into a T fitting, then off to the pump suction. All lines are 1 1/2" - so even if you decide to draw from the drain and the skimmer at the same time, you're contstrained by the 1 1/2" suction on the pump.

Old pump suction layout - skimmer bottom left, bottom drain top left, vacuum port top right, pump suction bottom right. 
I have 1 1/2" black poly pipe running underground to the pool. I'm not a huge fan of the insert barbed fittings - they're common for these applications but they neck the diameter down to 1 1/4 inch. I thought I would give a polyethelene epoxy adhesive a try, to convert to PVC fittings, made by TAP plastics in California.

Black poly lines moved to desired alignment, fixed with copper strapping. CPVC reducing slip elbows - 1 1/2" to 2" - fixed to the black poly line using TAP plastics poly epoxy.
I also converted the 1 1/2" poly lines to 2" at the 90 degree elbows where I made the transition from vertical to horizontal. See photo above. Once my suction lines were horizontal, I plotted the position of two Jandy 3 way valves facing each other, to allow me full flexibility in selecting and mixing the pump suction source. I used the 2 / 2 1/2" Jandy Valves to minimize restriction in the suction piping.

Suction side piping completed - Jandy Valves control suction source - skimmer, bottom drain, or vacuum port. 2" union fittings on the suction and discharge of the Jacuzzi Magnum pump. 
With the suction side piping completed - I then working on the transitions at the sand filter. I spent some time looking for a sand filter with a 2" multiport valve - mine was just a 1 1/2" multiport valve, and eventually decided just to keep the 1 1/2" valve. With the variable speed pump - the system would in the future be spending most of the time operating at a low flow speed, which would minimize the impact of the system restriction of the 1 1/2" multiport valve.

Jaccuzzi Multiport Sand Filter Valve Piping - 1 1/2" drain fitting on the close side, 2" rigid pipe discharging to the thermopump and salt cell on the far side. Pump discharge - sand filter feed line in the center. Unions on all connections. 
With the sand filter piped, it was time to work on the thermopump. The former layout had the thermopump piping side facing away from the pool shack, and 90 degrees away from the pool. In order to make the connections, about 30' of 1 1/2" hose made long circular connections between the sand filter and the salt cell.

The old Thermopump Installation - About 30' of 1 1/2" hose separates the Sand Filter from the connection to the underground hose where the Salt Cell will be attached to

The old Thermopump Installation - About 30' of 1 1/2" hose separates the Sand Filter from the connection to the underground hose where the Salt Cell will be attached to - right side of photo.
I moved the thermopump so that the piping connections would be facing the pool, and perpendicular to the pool shack, and then came up with a layout using the Jandy 3 way valves to control bypass and flow to the thermopump. 

The Thermopump was previously installed on the patio stones to the right. It's now moved into place next to the pool shack, just behind the outlet pipe for the pool jets. 

Jandy Valves will provide flow modulation and bypass isolation for the thermopump, with a much more compact piping arrangement.
Now, instead of 30' of 1 1/2" pipe between the sand filter and the salt cell, I'm down to about 10' of 2" pipe

Conclusions

I'm quite happy with the new piping arrangement and the upgrade to 2" piping. The only section of 1 1/2" pipe which remains is the section about 35' long between the salt cell and the first jet on the pool. I don't think I'll get the energy to make that upgrade for a while because of the trenching, so I'll wait until the pool requires major maintenance.

At this point, it was time to start the new variable speed motor - more on my next post.

Sources and Links

I hope you found this post useful. Feel free to ask questions in the comments section below. I answer all questions.

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Ecotech EZ Variable Speed Pool Pump Motor Upgrade - Jacuzzi Magnum Pump

I've been working towards the goal of reducing my electricity bill by 33% - and I'm actually getting there. One of the largest loads besides heating and ventilation at my house is the pool pump. I have a typical single speed 1.5 HP Jacuzzi Magnum pool pump for an 18' x 36" rectangular in-ground pool. I like to open the pool early and close it late, and the kids love to swim. My estimates for running the Jacuzzi Magnum pump was around $500 / pool season full time. I've been running the pump on a time, for about 12 hours / day - so I guess I've actually been consuming around $300 per year in electricity. Thankfully, my marginal electricity cost is only about $0.095/kW-hr.

Ecotech EZ Motor installed on the Jacuzzi Magnum 1500 Pool Pump. The control panel is directly on top of the motor.
Last year I did a fair amount of research on the subject. and the key to saving electricity with a pool is to take advantage of pumping affinity law - which simply means that increasing the flow by 10% costs you 33% more in power. Similarly, reducing the flow by 25% will result in energy savings of approximately 50% - due to the reduction in friction losses by reducing the speed of the water in the piping (and importantly, across your filter element).

You can do this with multi-speed pumps - which can be standard wound-rotor pumps with a two or three speed tap - which will result in some savings, or even more significantly, with a electronically commutated permanent magnet variable speed motor, which are the most efficient commercially available motors. To take advantage of this simple principle, the state of California has mandated that new pool installations have as a minimum multi-speed pumps which default to low speed operation for filtration (California Energy Commission (CEC) Title 20 Appliance Efficiency Regulations).

My pool is probably a fairly typical installation for a 20 year old pool in the Province of Quebec - all the piping is 1 1/2 inches in diameter, and I have a 1.5 HP single speed motor, with a sand filter with a 1 1/2 inch multiport valve. My thermopump was added following the original pool installation - and it would have been difficult to imagine a less efficient plumbing addition to a system - to add the Thermopump - the pipe from the sand filter to the pool was extended by about 30 feet long in total - 1 1/2" piping - in a long serpentine.

So why upgrade just the motor, and not purchase a complete new pump? Because if you already have a decent pump - the motor will end up costing about 50% of the cost of a complete pump. If you're a bit handy, this isn't a particularly difficult upgrade. The hardest part may be the electrical part - and if you're switching the complete pump out - you'll need to deal with that anyway. My aim going into this upgrade is that the cost for the upgrade would be paid back within 2 years, and purchasing a complete new pump would not allow me to achieve that.

Starting point - Jacuzzi Magnum Pump with Single Speed, Permanent Split Capacitor Motor
So - to take best advantage of the variable speed motor upgrade, I also planned to upgrade as much of my piping as possible to 2" diameter, and relocate my thermopump to optimize the piping arrangement. I also planned to remove and replace all my 1 1/2" ball valves with 2 inch Jandy multiport valves - to simplify the plumbing and minimize the number of bends in the piping.

The first step in the project was to split the original single speed motor from the pump, and install the Ecotech EZ motor. This isn't terribly difficult to do, and it is also an excellent opportunity to replace your pump seal. The basic steps are as follows:
  • remove the pump from your system and disconnect the power;
  • split the pump from the motor by unscrewing the clamp ring between the motor and the pump;
  • unscrew the 2 screws retaining the diffuser, and lift the diffuser off;
  • unscrew the impeller by holding the motor end of the drive shaft, and unscrewing the impellor counter clockwise; 
  • lift off the seal housing (now is the time you would replace the motor shaft seals); 
  • unbolt the motor housing bracket (four bolts)
Preparing the Motor Housing Bracket for installation on the new Ecotech Motor
Note the clamp ring installed over the motor, with the seal plate installed over the motor housing bracket and motor shaft
Installing the impeller
Installation of the new motor is the reverse of the steps above, I won't go into details, there's quite a few good videos available explaining seal replacement on all types of pool pumps. Just ensure you take very clear note of the orientation of all parts during disassembly - photos will help. And - make sure you install the clamp ring right from the start - otherwise you'll be doing all the steps twice....

The Ecotech EZ motor installed on the Jacuzzi Magnum 1500 Pump - Ready to Install on the Pool
I'll write a separate post on the piping upgrade around the pump, sand filter and thermopump, Following that, I'll post about wiring up the new pump, the electrical considerations, power draw of the new motor, and the performance of the system. It's getting a bit too late to finish everything tonight.






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Delta Vertical Wall Mount Bike Rack - from Lee Valley Tools

It's been a while since my last post - this spring has been exceptionally busy with the basement insulation project, basement floor slab crack repairs and concrete floor painting, the variable speed pool pump motor upgrade, and the 2" pool plumbing upgrade. I still have to write about the pool projects, but first I wanted to show some photos from my bike rack upgrade in the garage.

The completed installation - adult bikes mounted vertically on the wall - kids bikes parked underneath. Very space efficient, and easy for the kids.
The new house had a series of hooks on the ceiling - 10' off the floor, and over the railing next to the stairs to the basement. To lift a bike up or down from a hook, you would have to get close to the railing, and stretch to get the front or rear wheel on or off the hook on the ceiling - a real task. The bicycles would pivot on the hooks, and bang into each other - pretty frustrating at times. I wanted a solution that would keep the bikes off the floor - we need all the floor space to park 2 cars at times, and help keep the space neat.

The previous storage rack - bikes would swing around, handlebars would hook, not ideal.
I did a bit of research into vertical wall mount bike racks - there are some interesting designs - then I found these at Lee Valley Tools. The great thing about Lee Valley Tools - reasonable prices ($21 each), quick and inexpensive shipping (frequent free shipping promotions) and quick delivery. So - I ordered six and they arrived in 2 days.

Delta Cycles Vertical Bike Rack with Tire Tray
If you look at other vendors - sometimes they will sell the rack and the tire tray separately - the Lee Valley Tools packaging includes both for one price.

Mounting the racks was simple - I found my wall studs were spaced 16" - and decided to lay out all four racks for the adult bikes - 2 road bikes, 2 mountain bikes - on 16" centers with staggered heights so the handlebars wouldn't interfere with each other. 

First bike installed. I used a Laser Level to get the top and bottom trays vertically aligned. 
Here's a photo of all 4 bikes installed - 16" centers. This turned out to be perfect spacing. 12" spacing would not have been enough (although it might have worked if you need a very tight installation).

4 bikes - 16" centers
The bike hooks are solid, support the bikes well. I'm careful when installing the bikes on the hooks to let the weight down slowly on the hook, to make sure I don't over stress the wheel rim. The upper rack installs with two 1 1/2" screws provided with the kit. These screws are a bit too short if you're installing on a stud wall with drywall - you'll need longer hardware for a solid installation.

The supplied hardware is too short for drywalled walls - these screws are only suitable for mounting directly to wood studs.
Delta Bike Rack
And here's a photo of the bottom tray. The bottom tray mounts with self adhesive tape - no screws required although screw holes are provided.

Note the vintage green Michelin Wildgripper Sprint S tires - Kevlar beads, super light, and now getting very old and brittle. Time for new tires.....
In summary - good quality racks, very good price, simple installation, clean look when storing bikes - very satisfied with this system.








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Basement Concrete Floor Paint - Single Part Epoxy Paint

Our 25 year old house has (had) a concrete floor in the basement utility room that was a bit more than rough. A spiderweb of hairline cracks, and some surface abrasion / weakness caused by lack of maintenance and efflorescence in certain places. It looked like the concrete had been painted at one time, but it was very difficult to tell.

The completed floor paint job.

Concrete prepared for painting - all cracks filled with Sika Epoxy Crack Fill
With the basement insulation project, where all the perimeter walls had to be cleared so that the drywall could be removed, and spray polyurethane foam insulation applied - it was the perfect time to paint the perimeter of the concrete floor. Prior to paint, I repaired all the floor cracks with Sika Crack Fix - from hairline cracks to the largest cracks which measured approximately 4mm wide at their widest. 15 tubes of Sika Crack Fix - $300 worth of epoxy - and all the cracks were filled and the floor ready to paint.

Cracks repaired that run into floor sump
For a concrete floor paint job, I highly recommend that you have a belt sander - it's perfect for smoothing out any surface roughness, high spots on epoxy crack fill, and buffing out any surface imprefections due to efflorescence. Since I just need a belt sander for this project, I bought an inexpensive Skil 3 x 18" belt sander - the 6A 7510 with pressure control. It's a nice tool, and was perfect for this job.

For paint - I decided to go with a simple single part epoxy. I did not want to get into two part epoxies requiring mixing of part A and part B - since I wouldn't have any heavy loads or vehicles on the floor. I also wanted a brand name product with a good reputation, commonly available at local building stores - so that I could restock easily, and hopefully procure the same product for touchups every couple of years.

I settled on the Kilz single part epoxy concrete floor paint - reasonably priced and with good online reviews, from a good manufacturer.


Kilz Concrete and Garage Floor Paint
I had several spots with efflorescence - a white crystalline staining in several spots on the floor - particularly around 3 or 4 concrete columns supporting the garage elevated slab. I chose to simply wash the efflorescence with the concrete wash product recommended by the paint instructions - KILZ Concrete & Masonry Cleaner & Degreaser.

Following the first coat of paint, I found that any places I had raised epoxy repairs, and I hadn't sanded the epoxy - I didn't get a particularly good bond of the paint to the epoxy. So for some spots, I went back and sanded down the epoxy crack fills with the belt sander, which also roughened the epoxy and improved adhesion of the paint.

Sanding down Epoxy crack repairs flush with the concrete
I also found that where I had heavy efflorescence stains, and I only cleaned with the KILZ Concrete & Masonry Cleaner & Degreaser, the paint puffed up as it dried, and gave very poor adhesion. So it was clear - I had to do a better job dealing with the efflorescence prior to painting.

Halo of efflorescence around concrete column - led to poor adhesion.
At the spots where I had poor adhesion - I used the belt sander to take the paint back down to the concrete, and physically remove any efflorescence from the surface. Then I used the recommended concrete etching product - KILZ Concrete & Masonry Cleaner & Etcher. This product was aggressive on the efflorescence, and soaked into the porous surface of the concrete - bubbling and hissing whereever it encountered the efflorescence. I then cleaned with rinse water, and let dry for 24 hours. When I went back to inspect the concrete - the concrete was perfectly clean, dry and natural coloured, except in a few spots where there was some new white efflorescence on the surface of the concrete - much less than before. So at these spots - I did a second treatment with the KILZ Concrete & Masonry Cleaner & Etcher, and waited another 24 hours. Following the second treatment, I had no further efflorescence on the surface of the concrete.

Efflorscence repair - sand down the paint, remove the efflorescence with Concrete Etch, and repair weak surfaces with a thin layer of Sika Epoxy Crack Fix
So - I then applied a second coat of paint - and so far - it seems to have beat the efflorescence, no puffiness or lack of adhesion in the paint, and better bonding of the paint to the epoxy crack fix.

Finally - I had spots of the concrete floor where there were small sections - up to a foot long by 6 inches wide - where the surface of the concrete had started crumbling slightly, leaving a rough surface. At these spots, I used Sika Crack Fix applied across the surface, spread out with a putty knife, and sanded flat with the belt sander once cured. This protected the concrete surface, and gave a nice smooth surface for the paint to adhere to.

Rough surface repair with Sika Epoxy Crack Fix - levels chips 
The final product look much much cleaner, and neat. A huge improvement. A bit of an investment in time and effort, but I think it should pay off when it comes time to sell the house.

Final floor repair


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Basement Floor Slab - Horizontal Crack Repairs using Sika Crack Fix

The past three weeks we've been upgrading the basement foundation wall insulation - so I've had to move all the shelving and storage units away from the basement walls to get at the walls. Since all the heavy lifting was done to move everything away from the walls, I decided it was an excellent opportunity to give the concrete floors a coat of paint. Prior to painting, it was the perfect time to repair the horizontal cracks in the concrete slab - so I've been at this in parallel with the insulation job.

Final Crack Repair - Sika Crack Fix
Following some reasearch - I've settled on using Sika Crack Fix - a structural epoxy that is very fluid and can penetrate very narrow cracks, and is also commonly available at my local home improvement stores. It's not inexpensive, at about $20 a tube, but if I can get a permanent repair to these slab cracks I'll be satisfied.

Sika Crack Fix - Comes in a Cartridge designed for a standard small caulking gun, with two mixing tips. 

Cartridge installed in the caulking gun
The first step to a smooth repair is to open up the top of the cracks with an angle grinder and a concrete wheel. Create a groove at the top of the crack - 2 to 4 mm wide - and relatively straight - this will create a channel that will make the application of the epoxy much easier, and create a small well for the epoxy to pool before it penetrates the crack. This is the key to a neat, easy crack repair. When creating the groove with the grinder, use your shop vac with the hose end held right next to the grinder wheel, this will pick up 95% of the dust, and help keep your work area clean.

Groove the top of your cracks with an angle grinder prior to application of the epoxy
Once the cracks have been grooved, you can start applying the epoxy. Since I have no way of plugging the crack at the bottom of the slab - the epoxy is so thin it will run right down through the crack, and out the bottom of the slab. To minimize waste, I would apply one or two tubes of Sika Crack Fix to about 25 feet of prepared cracks - and allow the epoxy to penetrate the cracks. I would then wait 24 hours and repeat the process - to allow the crack to shrink in width over subsequent applications and minimize the leakage out the bottom of the crack.

Once the crack is filling up - you'll find that the epoxy will run horizontally as well - moving down any slope in the floor slab. This isn't a problem, it helps to distribute the epoxy fully through the crack, but you may find that some epoxy will pool out of the crack on the surface of the floor. The hardened epoxy is so hard that it is difficult to remove by scraping or sanding. After about 4 to 6 hours following the application of the epoxy - the epoxy will set up and start to harden - yet it will still be soft enough to scrape off any unwanted excess. This is an excellent time to level out any sections where the epoxy is convex - and extending above the surface of the surrounding floor. 

Completed crack repair - where the epoxy has been scraped flat before completely hardening. 
The Sika Crack Fix can also be used to fix broken surfaces - I have some small areas around a floor sump where the concrete surface has chipped away slighly exposing some aggregate. I've been using the Sika Crack Fix to smooth these areas prior to painting.

Wider surface repairs using Sika Crack Fix - This section is still slightly concave, and will require a subsequent application of Crack Fix to get it flat. 
I've used about 10 tubes of the Sika Crack Fix in about 40 feet of narrow cracks averaging about 1mm wide. That's a bit expensive at $20 a tube - but if it does a "permanent" long term repair - I'll be happy with that. It looks like the epoxy will have to be roughened prior to painting with sandpaper - if left to settle on its own it hardens very smooth - almost glass like, and I'll be looking for good adhesion with the floor paint. I'll post on the floor paint process later, as I get that task done.

Now - for a few other points now that I've almost finished all the crack repairs in the basement.

Sometimes, the part A and part B doesn't mix correctly, and won't harden in the crack. This may happen at the start of the tube, at the end of the tube, or if you interrupt application and restart with a new mixing tip. The instructions for the product suggest pouring out product in a waste container until all the air bubbles are gone - this ensures the product being applied has a proper mix of both components - and is very important. When you get to the end of the tube, and the mixing tube starts spouting bubbles - stop there and discard the tube. I've had a few instances where the product hasn't mixed correctly, and the epoxy stays sticky and doesn't harden. You can use a putty knife or rag to scrape off as much of this material as possible, and then finish cleanup with a solvent. The product guide recommends "Sika Equipment Cleaner" to clean up unmixed or uncured epoxy.  This product contains Xylene according to the MSDS, and so does the brake cleaner that I had in my garage, so I've cleaned some of this unmixed epoxy with a small amount of brake cleaner. (Try getting some "Sika Equipment Cleaner" on a Sunday morning....)

Unmixed epoxy cleaned up with Brake Cleaner, ready for re-application of mixed Crack Fix
Another issue that I ran into is that the Crack Fix is so watery when applied, it flows with any slight slope in the concrete slab. I have a few cracks that extend to a floor sump, with a slight grade. The crack fix kept on flowing along the crack, and leaving a trough in the crack, and puddling out of the crack at the bottom of the slope. The solution to this is to shoot some Crack Fix into a small plastic container, and let it set for 2 to 3 hours. Once the product starts setting up, and not flowing, apply it to the crack with a putty knife. It should stay in the crack without flowing down. Check and retrowel with the putty knife after 30 minutes.

Crack Fix setting up in a plastic cap, almost ready to apply.
Finally, in preparation for painting, I've found that a belt sander is really the best way to level out cracks. I had always managed to get by without a belt sander until now. I went out, purchased an inexpensive Skil 3 x 18 sander, and a few belts of 80 grit. This machine works great for levelling out the cracks and getting a nice flat surface equal with the concrete prior to painting. 

Skil 7510-01 3 x 18" belt sander, with vacuum attached. Perfect for levelling epoxy Crack Fix.
The sander accepts a 1 1/2" shop vac hose for dust collection, which also helps remove heat from the motor during operation. I highly recommend operating this tool with a vacuum attached. It's really efficient at levelling out cracks.

Epoxy filled cracks levelled with the belt sander, ready for painting. 
This has been a good job to get done - so far, I've used about a dozen tubes of Crack Fix. It's not inexpensive, but compared to bringing in a conctractor to replace your basement floor slab, this is an excellent way to prolong the life of your basement floor.

Getting near the end of the job. Perimeter of the floor - painting completed. Now filling all the cracks in the center of the floor, almost ready to complete the painting. 









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